Birgenair Flight 301

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Birgenair Flight 301
Birgenair Boeing 757-225; TC-GEN@FRA;19.10.1994 (4704783314).jpg
The aircraft involved in the accident on 19 October 1994
Accident
Date6 February 1996 (1996-02-06)
Summary Stalled and crashed into the ocean
Site26 km (16 mi; 14 nmi) NE of Gregorio Luperón International Airport
Puerto Plata, Dominican Republic
19°54′50″N70°24′20″W / 19.91389°N 70.40556°W / 19.91389; -70.40556
Aircraft
Aircraft type Boeing 757-225
Operator Birgenair
IATA flight No.KT301
ICAO flight No.ALW301
Call signALPHA LIMA WHISKY 301
Registration TC-GEN
Flight origin Gregorio Luperón International Airport
Puerto Plata, Dominican Republic
1st stopover Gander International Airport
Gander, Newfoundland and Labrador, Canada
2nd stopover Berlin Schönefeld Airport
Berlin, Germany
Destination Frankfurt Airport
Frankfurt, Germany
Occupants189
Passengers176
Crew13
Fatalities189
Survivors0

Birgenair Flight 301 was a flight chartered by Turkish-managed Birgenair partner Alas Nacionales from Puerto Plata in the Dominican Republic to Frankfurt, Germany, via Gander, Canada, and Berlin, Germany. On 6 February 1996, the Boeing 757-200 operating the route crashed shortly after take-off from Puerto Plata's Gregorio Luperón International Airport, killing all 189 people on board. [1] [2] [3] The cause was pilot error after receiving incorrect airspeed information from one of the pitot tubes, which investigators believe was blocked by a wasp nest built inside it. The aircraft had been sitting unused for 20 days, and without pitot tube covers in place for the two days preceding the crash.

Contents

Flight 301 is the joint-deadliest aviation incident involving a Boeing 757 (along with American Airlines Flight 77) having a total of 189 fatalities. Furthermore, Flight 301 is the deadliest aviation accident ever to have occurred in the Dominican Republic. [4] Before 1995, the deadliest aviation accident in the Dominican Republic was the crash of a Dominicana de Aviacion DC-9 in 1970, which killed 102.

Aircraft and crew

The aircraft was a 12-year-old Boeing 757-225, registered as TC-GEN, with a manufactured serial number of 22206. The plane's line number was 31. It was powered by two Rolls-Royce RB211-535E4 engines.[ citation needed ]

The crew consisted of 11 Turks and 2 Dominicans. The captain was Ahmet Erdem (61), with 24,750 flight hours of experience (including 1,875 hours on the Boeing 757). The first officer was Aykut Gergin (34). He had 3,500 hours of flying experience, though only 71 hours were on the Boeing 757. The relief pilot was Muhlis Evrenesoğlu (51). He had 15,000 flight hours of experience (with 121 of them on the Boeing 757). [5] :4–8

Passengers

The passengers consisted mainly of Germans, along with nine Poles including two Members of the Parliament, Zbigniew Gorzelańczyk of the Democratic Left Alliance, and Marek Wielgus of the Nonpartisan Bloc for Support of Reforms (BBWR). [2] [6] Most of the passengers had booked Caribbean package holidays with Öger Tours; Birgenair held 10% of Öger Tours. [7]

NationalityPassengersCrewTotal
Flag of Germany.svg  Germany 167-167
Flag of Poland.svg  Poland 9-9
Flag of Turkey.svg  Turkey -1111
Flag of the Dominican Republic.svg  Dominican Republic -22
Total17613189

Accident

National Transportation Safety Board (NTSB) animation of Flight 301's takeoff and accident

During takeoff roll at 23:42 AST (03:42 UTC), [5] :1 the captain found that his airspeed indicator (ASI) was malfunctioning but he chose not to abort the takeoff. [8] The first officer's ASI was functional, though subsequent warning indicators caused the aircrew to question its veracity as well. The aircraft took off normally at 23:42 AST for the first leg of the flight. At 2,500 feet (760 m), the flight switched to main air traffic control and was instructed to climb to flight level 280 (28,000 ft or 8,500 m). The autopilot was engaged 1 minute and 30 seconds into the flight.

Approximately 10 seconds later, two warnings—rudder ratio and Mach airspeed trim—appeared. The crew was at that point becoming increasingly confused because the captain's ASI showed over 300 knots (560 km/h; 350 mph) and increasing, and the first officer's ASI, which was correct, was showing 220 knots (410 km/h; 250 mph) and decreasing.

Then, the captain assumed that both ASI were wrong and decided to check circuit breakers. When the first circuit breaker was checked, the overspeed warning appeared, as the captain’s ASI, the primary source of the information about airspeed for autopilot, was showing airspeed near 350 knots (650 km/h; 400 mph) and increasing. Then the second circuit breaker was pulled to silence the warning. As the plane was climbing through 4,700 feet (1,400 m), the captain's ASI read 350 knots (650 km/h; 400 mph). The autopilot, which was taking its airspeed information from the same equipment that was providing faulty readings to the captain's ASI, increased the pitch-up attitude and reduced power in order to lower the plane's airspeed. The first officer's ASI was giving a correct reading of 200 knots (370 km/h; 230 mph) and was still decreasing. [5] :16 With all contradictory warnings given by the plane, the confused captain decided to reduce thrust of the plane, believing it was flying too fast. [5] :18

This action immediately triggered the 757's stick shaker stall alert, warning the confused pilots that the aircraft was flying dangerously slow. Also, the autopilot disengaged. As the plane was close to a stall, its path became unstable and it started descending. Meanwhile, the controller, still unaware of any problems, called the flight, but, as the crew struggled with problems, the first officer said, "Stand by". The first officer and relief pilot, aware of the scale of the problem, were suggesting various methods to recover from the stall, but the confused captain ignored all of them. About 20 seconds before crash, the captain finally attempted to recover from the stall by increasing the plane's thrust to full, but as the aircraft was still in a nose up attitude, the engines were prevented from receiving adequate airflow required to match the increase in thrust. The left engine flamed out, causing the right engine, which was still at full power, to throw the aircraft into a spin. Moments later, the plane inverted. [9] At 23:47 AST, the Ground Proximity Warning System (GPWS) sounded an audible warning, and eight seconds later the plane crashed into the Atlantic Ocean. All 176 passengers and 13 crew members died on impact.

Investigation and final report

Memorial for the victims of Birgenair Flight 301 in Puerto Plata Ppaircrashmemorial.JPG
Memorial for the victims of Birgenair Flight 301 in Puerto Plata
Memorial for the victims of Birgenair Flight 301 in Frankfurt's main cemetery Birgenair-mahnmal.jpg
Memorial for the victims of Birgenair Flight 301 in Frankfurt's main cemetery

The Dominican Republic government's General Directorate of Civil Aviation (Spanish : Dirección General de Aeronáutica Civil) (DGAC) investigated the accident and determined the probable cause to be: [10]

The crew's failure to recognize the activation of the stick shaker as a warning of imminent entrance to the stall, and the failure of the crew to execute the procedures for recovery from the onset of loss of control.

Investigations later showed that the plane was actually travelling at 220 knots (410 km/h; 250 mph) at the time of the accident. [5] The investigation concluded that one of the three pitot tubes, used to measure airspeed, was blocked.

None of the pitot tubes were recovered so investigators were unable to determine for certain what caused the blockage. Investigators believe that the most likely culprit was the black and yellow mud dauber (Sceliphron caementarium), a type of solitary sphecid wasp well known to Dominican pilots, which makes a cylindrical nest out of mud and tends to establish a nest in artificial, cylindrical structures. According to the final report, section 2.3 – "Aircraft maintenance factors", the aircraft had not flown in 20 days; however, this was not the duration for which pitots remained uncovered, but there was evidently enough time to allow the wasps the opportunity to construct nests in the tubes. [5] :20 [11] [12] According to Cetin Birgen, president and CEO of Birgenair, the pitot covers were removed two days before the accident in order to conduct an engine test run. [5] :20 [13]

The investigation noted a number of other factors and suggested changes. [8] They reconfirmed that the pilots should have followed existing procedures and aborted the takeoff when they found that their airspeed indicators were already in significant disagreement as the plane accelerated down the runway. Results from a number of simulations with experienced pilots found that the combination of the overspeed warning horn and underspeed stick shaker while in flight was an overly confusing contradictory set of messages for many pilots; the FAA issued a directive that pilot training would now include a blocked pitot tube scenario. The FAA research had also revealed that the situation also led to multiple other contradictory warning sounds and warning lights that increased the demands on the pilot to fly the plane. The FAA asked Boeing to change some of those warnings, as well as add a new warning to tell both pilots that their instruments disagree, add the ability for the pilots to silence troublesome alarms, and to modify the system so that the pilots can choose which pitot tube the autopilot uses for airspeed readings. [8]

Aftermath

Shortly after the crash of Flight 301, the airline's overall image and profits became heavily damaged, and some of its planes were grounded at the same time. Birgenair went bankrupt in October of the same year as there were concerns about safety after the accident, causing a decline in passenger numbers. The crash and ensuing negative publicity both contributed to Birgenair's bankruptcy. [14]

See also

Similar events

References

Citations

  1. Pope, Hugh (10 February 1996). "Crash plane may not have been serviced". The Independent . Retrieved 19 November 2009.
  2. 1 2 "Rescuers call off search in plane crash". CNN . 8 February 1996. Archived from the original on 13 April 2005. Retrieved 19 November 2009.
  3. Wald, Matthew L. (8 February 1996). "German Tourist Plane Crashes; 189 Feared Dead". The New York Times. ISSN   0362-4331 . Retrieved 26 January 2021.
  4. Accident description at the Aviation Safety Network . Retrieved on 21 July 2006.
  5. 1 2 3 4 5 6 7 "Reporte Final Accidente Aereo Birgenair, Vuelo ALW-301, Febrero 06,1996" [Final Report of the Birgenair Air Crash, Flight ALW-301, 6 February 1996](PDF) (in Spanish). DGAC. 25 October 1996. Archived (PDF) from the original on 3 March 2016. Retrieved 27 August 2014.
  6. Clary, Mike (8 February 1996). "Dominican Jet Crashes in Sea; 189 Feared Dead". Los Angeles Times. Retrieved 25 February 2018.
  7. Karacs, Imre (9 February 1996). "Bonn grounds 757 as crash mystery grows". The Independent. Retrieved 19 November 2009.
  8. 1 2 3 4 "Mixed Signals". Mayday . Season 5. Episode 8. 2007. Discovery Channel Canada / National Geographic Channel.
  9. Beveren, Tim van (1996). Runter kommen sie immer: die verschwiegenen Risiken des Flugverkehrs [They always come down: the hidden risks of air traffic] (in German). Campus-Verlag. pp. 258–271. ISBN   978-3-593-35254-1.
  10. Walters, James M.; Sumwalt III, Robert L. (16 February 2000). Aircraft Accident Analysis: Final Reports. McGraw Hill Professional. p. 98. ISBN   978-0-07-137984-7 . Retrieved 11 May 2011 via Google Books. Souffront, Emmanuel T., Presidente, Junta Investigadora de Accidentes Aéreos (JIAA) of the Director General of Civil Aviation (DGAC) of the Dominican Republic. 1996. Aircraft accident information. Dominican Republic Press Release—Factual Information, 1 & 18 March 1996.
  11. "Erroneous airspeed indications cited in Boeing 757 control loss" (PDF). Flight Safety Foundation. October 1999. p. 2. Retrieved 27 August 2014. It had not been flown for 20 days before the accident...Investigators believe that the engine [covers] and pitot covers were not installed before or after the engine ground test.
  12. DGAC final report 1996, p. 20, section 2.3"Durante el tiempo que duró en tierra, dicho avión no fue volado en veinte (20) dias. Durante este periodo se ejecutó una inspección de motores que requirió una prueba en tierra del motor antes del despegue. Los investigadores creen que las cubiertas de los motores y cubiertas de los pitot no fueron instaladas antes ó después de la prueba en tierra de los motores. [English: During the time that the aircraft was on the ground, it is believed that the plane had not flown for twenty (20) days. During this period, an engine inspection was performed that required an engine ground test before the next takeoff. Investigators believe that the engine and pitot covers were not installed before or after the engine ground test.]"
  13. Birgenair comments 1996, pp. 16–17"the aircraft was not on the ground for 20 days, but only for 12 days prior to the ill-fated flight. The pitot-tubes were covered prior to an engine test run which took place 2 days prior to the ill-fated flight. It was known by the BIRGENAIR mechanics that the airplane should be returned to Turkey in a ferry flight within the next 3 days. If therefore the pitot-tubes had not been covered after the engine test run for 2 days, according to the BOEING procedures, set forth in the BOEING Maintenance Manual, this might be justified." ... "Despite these irritating and even conflicting procedures set forth in BOEING's 757 Maintenance Manual and the Maintenance Planning Document, a blockage of the pitot-tube might occur even within any period of stay on the ground and [installation of pitot-covers] should therefore be clearly required for all periods of stay on the ground."
  14. Roelen, Alfred Lambertus Cornelis (2008). Causal Risk Models of Air Transport: Comparison of User Needs and Model Capabilities. IOS Press. p. 39. ISBN   978-1-58603-933-2.

Bibliography

External image
Searchtool.svg Pre-crash photos of the 757 carrying Flight 301 on Airliners.Net

Birgenair Flight 301 Monument Puerto Plata