Accident | |
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Date | 6 February 1996 |
Summary | Stalled and crashed into the ocean |
Site | 26 km (16 mi; 14 nmi) NE of Gregorio Luperón International Airport Puerto Plata, Dominican Republic 19°54′50″N70°24′20″W / 19.91389°N 70.40556°W |
Aircraft | |
Aircraft type | Boeing 757-225 |
Operator | Birgenair |
IATA flight No. | KT301 |
ICAO flight No. | ALW301 |
Call sign | ALPHA LIMA WHISKY 301 |
Registration | TC-GEN |
Flight origin | Gregorio Luperón International Airport Puerto Plata, Dominican Republic |
1st stopover | Gander International Airport Gander, Newfoundland and Labrador, Canada |
2nd stopover | Berlin Schönefeld Airport Berlin, Germany |
Destination | Frankfurt Airport Frankfurt, Germany |
Occupants | 189 |
Passengers | 176 |
Crew | 13 |
Fatalities | 189 |
Survivors | 0 |
Birgenair Flight 301 was a flight chartered by Turkish-managed Birgenair partner Alas Nacionales from Puerto Plata in the Dominican Republic to Frankfurt, Germany, via Gander, Canada, and Berlin, Germany. On 6 February 1996, the Boeing 757-200 operating the route crashed shortly after take-off from Puerto Plata's Gregorio Luperón International Airport, killing all 189 people on board. [1] [2] [3] The cause was pilot error after receiving incorrect airspeed information from one of the pitot tubes, which investigators believe was blocked by a wasp nest built inside it. The aircraft had been sitting unused for 20 days, and without pitot tube covers in place for the preceding two days before the crash.
Flight 301 is the joint-deadliest aviation incident involving a Boeing 757 (along with American Airlines Flight 77) having a total of 189 fatalities. Furthermore, Flight 301 is the deadliest aviation accident ever to have occurred in the Dominican Republic. [4] Before 1995, the deadliest aviation accident in the Dominican Republic was the crash of a Dominicana de Aviacion DC-9 in 1970.
The aircraft was a 12-year-old Boeing 757-225, registered as TC-GEN, with a manufactured serial number of 22206. The plane's line number was 31, and it had flown its maiden flight on 3 February 1984. [5] It was originally delivered to Eastern Air Lines on 26 February 1985 and registered as N516EA. It was powered by two Rolls-Royce RB211-535E4 engines. After Eastern Air Lines' bankruptcy and subsequent liquidation in 1991, the aircraft was stored at the Mojave Air and Space Port for more than a year. It was purchased by Aeronautics Leasing in April 1992, then leased to Canadian airline Nationair in May 1992, and stayed with the airline until its demise the following year. It was leased again by the same lessor in July 1993 to Birgenair and then sub-leased to International Caribbean Airways in December 1994, and Birgenair operated the airliner until it crashed. [6]
The crew consisted of 11 Turks and 2 Dominicans. The captain was Ahmet Erdem (61), with 24,750 flight hours of experience (including 1,875 hours on the Boeing 757). The first officer was Aykut Gergin (34). He had 3,500 hours of flying experience, though only 71 hours were on the Boeing 757. The relief pilot was Muhlis Evrenesoğlu (51). He had 15,000 flight hours of experience (with 121 of them on the Boeing 757). [7] : 4–8
The passengers consisted mainly of Germans, along with nine Poles including two Members of the Parliament, Zbigniew Gorzelańczyk of the Democratic Left Alliance, and Marek Wielgus of the Nonpartisan Bloc for Support of Reforms (BBWR). [2] [8] Most of the passengers had booked Caribbean package holidays with Öger Tours; Birgenair held 10% of Öger Tours. [9]
Nationality | Passengers | Crew | Total |
---|---|---|---|
Germany | 167 | - | 167 |
Poland | 9 | - | 9 |
Turkey | - | 11 | 11 |
Dominican Republic | - | 2 | 2 |
Total | 176 | 13 | 189 |
During takeoff roll at 23:42 AST (03:42 UTC), [7] : 1 the captain found that his airspeed indicator (ASI) was malfunctioning but he chose not to abort the takeoff. [10] The first officer's ASI was functional, though subsequent warning indicators caused the aircrew to question its veracity as well. The aircraft took off normally at 23:42 AST for the first leg of the flight. At 2,500 feet (760 m), the flight switched to main air traffic control and was instructed to climb to flight level 280 (28,000 ft or 8,500 m). The autopilot was engaged 1 minute and 30 seconds into the flight.
Approximately 10 seconds later, two warnings—rudder ratio and Mach airspeed trim—appeared. The crew was at that point becoming increasingly confused because the captain's ASI showed over 300 knots (560 km/h; 350 mph) and increasing, and the first officer's ASI, which was correct, was showing 220 knots (410 km/h; 250 mph) and decreasing.
Then, the captain assumed that both ASI were wrong and decided to check circuit breakers. When the first circuit breaker was checked, the overspeed warning appeared, as the captain’s ASI, the primary source of the information about airspeed for autopilot, was showing airspeed near 350 knots (650 km/h; 400 mph) and increasing. Then the second circuit breaker was pulled to silence the warning. As the plane was climbing through 4,700 feet (1,400 m), the captain's ASI read 350 knots (650 km/h; 400 mph). The autopilot, which was taking its airspeed information from the same equipment that was providing faulty readings to the captain's ASI, increased the pitch-up attitude and reduced power in order to lower the plane's airspeed. The first officer's ASI was giving a correct reading of 200 knots (370 km/h; 230 mph) and was still decreasing. [7] : 16 With all contradictory warnings given by the plane, the confused captain decided to reduce thrust of the plane, believing it was flying too fast. [7] : 18
This action immediately triggered the 757's stick shaker stall alert, warning the confused pilots that the aircraft was flying dangerously slow. Also, the autopilot disengaged. As the plane was close to a stall, its path became unstable and it started descending. Meanwhile, the controller, still unaware of any problems, called the flight, but, as the crew struggled with problems, the first officer said, "Stand by". The first officer and relief pilot, aware of the scale of the problem, were suggesting various methods to recover from the stall, but the confused captain ignored all of them. About 20 seconds before crash, the captain finally attempted to recover from the stall by increasing the plane's thrust to full, but as the aircraft was still in a nose up attitude, the engines were prevented from receiving adequate airflow required to match the increase in thrust. The left engine flamed out, causing the right engine, which was still at full power, to throw the aircraft into a spin. Moments later, the plane inverted. [11] At 23:47 AST, the Ground Proximity Warning System (GPWS) sounded an audible warning, and eight seconds later the plane crashed into the Atlantic Ocean. All 176 passengers and 13 crew members died on impact.
The Dominican Republic government's General Directorate of Civil Aviation (Spanish : Dirección General de Aeronáutica Civil) (DGAC) investigated the accident and determined the probable cause to be: [12]
The crew's failure to recognize the activation of the stick shaker as a warning of imminent entrance to the stall, and the failure of the crew to execute the procedures for recovery from the onset of loss of control.
Investigations later showed that the plane was actually travelling at 220 knots (410 km/h; 250 mph) at the time of the accident. [7] The investigation concluded that one of the three pitot tubes, used to measure airspeed, was blocked.
None of the pitot tubes were recovered so investigators were unable to determine for certain what caused the blockage. Investigators believe that the most likely culprit was the black and yellow mud dauber (Sceliphron caementarium), a type of solitary sphecid wasp well known to Dominican pilots, which makes a cylindrical nest out of mud and tends to establish a nest in artificial, cylindrical structures. According to the final report, section 2.3 – "Aircraft maintenance factors", the aircraft had not flown in 20 days; however, this was not the duration for which pitots remained uncovered, but was evidently enough time to allow the wasps the opportunity to construct nests in the tubes. [7] : 20 [13] [14] According to Cetin Birgen, president and CEO of Birgenair, the pitot covers were removed two days before the accident in order to conduct an engine test run. [7] : 20 [15]
The investigation noted a number of other factors and suggested changes. [10] They reconfirmed that the pilots should have followed existing procedures and aborted the takeoff when they found that their airspeed indicators were already in significant disagreement as the plane accelerated down the runway. Results from a number of simulations with experienced pilots found that the combination of the overspeed warning horn and underspeed stick shaker while in flight was an overly confusing contradictory set of messages for many pilots; the FAA issued a directive that pilot training would now include a blocked pitot tube scenario. The FAA research had also revealed that the situation also led to multiple other contradictory warning sounds and warning lights that increased the demands on the pilot to fly the plane. The FAA asked Boeing to change some of those warnings, as well as add a new warning to tell both pilots that their instruments disagree, add the ability for the pilots to silence troublesome alarms, and to modify the system so that the pilots can choose which pitot tube the autopilot uses for airspeed readings. [10]
Shortly after the crash of Flight 301, the airline's overall image and profits became heavily damaged, and some of its planes were grounded at the same time. Birgenair went bankrupt in October of the same year as there were concerns about safety after the accident, causing a decline in passenger numbers. The crash and ensuing negative publicity both contributed to Birgenair's bankruptcy. [16]
A pitot tube measures fluid flow velocity. It was invented by French engineer Henri Pitot in the early 18th century, and modified to its modern form in the mid-19th century by Henry Darcy. It is widely used to determine the airspeed of aircraft; the water speed of boats; and the flow velocity of liquids, air, and gases in industry.
The airspeed indicator (ASI) or airspeed gauge is a flight instrument indicating the airspeed of an aircraft in kilometres per hour (km/h), knots, miles per hour (MPH) and/or metres per second (m/s). The recommendation by ICAO is to use km/h, however knots (kt) is currently the most used unit. The ASI measures the pressure differential between static pressure from the static port, and total pressure from the pitot tube. This difference in pressure is registered with the ASI pointer on the face of the instrument.
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Souffront, Emmanuel T., Presidente, Junta Investigadora de Accidentes Aéreos (JIAA) of the Director General of Civil Aviation (DGAC) of the Dominican Republic. 1996. Aircraft accident information. Dominican Republic Press Release—Factual Information, 1 & 18 March 1996.
It had not been flown for 20 days before the accident...Investigators believe that the engine [covers] and pitot covers were not installed before or after the engine ground test.
External image | |
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Pre-crash photos of the 757 carrying Flight 301 on Airliners.Net |
Birgenair Flight 301 Monument Puerto Plata